Lloyd_E
Veteran Member
- Joined
- Nov 15, 2003
- Messages
- 1,417
- Location
- South Shore Nova Scotia Canada
- Tractor
- 2008 Kioti DK 45 sc
Background - not sure if it applies: I had a 500+ hour service done a few weeks ago. New hydraulic filter and oil, new motor oil filter and oil. They didn't replace the fuel filter because they forgot to bring one.
Today I was chipper alders - nothing over 3" for about 2.5 hours. Not very hot today and temp gauge ran on the cool side. A few times the chipper got clogged and I would disengage and clean unit. Twice the engine idled down and just stall. Would start up and run fine.
Tonight I was returning from my buddies place down the road. Normally I would gear down to 3rd for this particular hill - I did and the tractor bogged down with no power. I shifted to 2nd and just barely made it up the hill. I continued on flat area of road and turned on to my lane. Same thing happened. I had to shift down to 3rd and 2nd - no amount of pedal could get rpm up. I stopped mid way up lane and started in 1st - shifted to second no problem.
Everything appears to be running smoothly. I am obviously missing something. Any insight?
TIA
PS: Along flat it accelerated fine up to my usual 2300 rpm 4th gear commute.
PPS: They adjusted clutch and brake linkage as well during the service.
Today I was chipper alders - nothing over 3" for about 2.5 hours. Not very hot today and temp gauge ran on the cool side. A few times the chipper got clogged and I would disengage and clean unit. Twice the engine idled down and just stall. Would start up and run fine.
Tonight I was returning from my buddies place down the road. Normally I would gear down to 3rd for this particular hill - I did and the tractor bogged down with no power. I shifted to 2nd and just barely made it up the hill. I continued on flat area of road and turned on to my lane. Same thing happened. I had to shift down to 3rd and 2nd - no amount of pedal could get rpm up. I stopped mid way up lane and started in 1st - shifted to second no problem.
Everything appears to be running smoothly. I am obviously missing something. Any insight?
TIA
PS: Along flat it accelerated fine up to my usual 2300 rpm 4th gear commute.
PPS: They adjusted clutch and brake linkage as well during the service.