Speaking of maintenance runs... it's been awhile since I pulled out my 6hp Merc outboard motor. I think I shall do that today.
Collateral Maintenance happening..... I'm cool with that !
Rgds, D.
Speaking of maintenance runs... it's been awhile since I pulled out my 6hp Merc outboard motor. I think I shall do that today.
Do you fog your outboard or other fueled equipment at the end of the season?
At one time that was what everyone recommended... don't hear about anymore.
On a separate note...
Looks like the commercial 2 stroke Toro mower came out unscathed from a half tank of straight fuel.
Posted that it ran out of fuel and there was a little straight gas in a can that used to fill it half way...
Excellent Compression and sounds good when I added some Stihl Ultra to the tank.
Maybe 25 years of two-stroke fuel left enough residue for 10 minutes of run time?
I知 currently in the process of repairing a 10hp Yanmar diesel clone in a generator that has 220 hours on the meter.
It was purchased for home backup and was being used on a job for 3 weeks running skil saws, sawzalls, a compressor and battery chargers.
It had run fine for weeks approx. 8 to 10 hrs. a day when it started skipping, blue smoke and various noises.
When I received it I tried to start it but it appeared to be low on compression and would not fire.
I pulled the oil filter screen and it was full of junk & sludge.
The owner said he wasn't aware of the filter because the manual got ruined in his cellar due to moisture where the generator is stored.
Further inspection and details of how the owner operated it indicates it may have been wet stacked from running in the winter with not enough load to warm it up.
I removed the engine & disassemble it and found 3 patches of rust on the cylinder wall but no scoring.
The exhaust port was wet from running with little load.
I removed the piston & rings which look good with no obvious defects along with all other components.
There were some deposits in the bottom of the crankcase but nothing serious.
I remove the valves from the head and saw some pitting on the exhaust seat so I cut new valve seats with my Neway seat cutter. I resurfaced the head on my granite surface plate using 220 wet/dry carbide paper.
Cylinder was honed which removed the patches of rust but pits in the cylinder wall remain which should be ok.
New parts installed are;
Piston rings, pto main bearing, rod bearing oil filter screen and various gasket & seals.
The block is built and the head is on and I'm trying to torque the flywheel nut to 150lbft of torque, I don't have the moxie anymore and I need to find some young muscle to help.
Further discussions with the owner indicate that he has no idea how much load he can put on it.
During an outage in the winter he basically runs the circulators for his hot water boiler (heat) and some lights which may total 1kw at best.
Will update as progress is made.
90cummins
Your shop needs some more resources.... or do you have a casting foundry out back too ?:laughing:
Thorough rebuild - thanks for the details. IMO, diesels suffer the worst from under-loading - good example of the consequences.
From your description of the sludge and rust, it sounds like the oil was neglected too.
Post-rebuild, I hope your buddy has learned a lesson, and adds a couple of space heaters as load.
Pls let us know how fire-up and run-in/testing goes.
Rgds, D.