So the current status is that with a three foot long wire and spade connectors I was able to go directly from the switch's crank terminal to the solenoid. Starts just fine, (so turns out the switch is ok) but of course I have bypassed all the safety stuff by doing so. Tried to trace the circuit from the switch to the solenoid, but that is going to require an evening in the shop as it goes all over the place. Either the broken wire/ bad connection issue is what it is, or could be something with a safety switch in that circuit. I must admit, I would have no idea about adjusting a safety switch (assuming mine has that type hiding in the rats nest of wiring harness in there). The idea of a switch with adjustable contacts or some kind of sensitivity setting would never have occurred to me in a million years, so thanks for the heads up. Seeing as dad always used really really old equipment I feel pretty confident that I can avoid trying to crank it without depressing the clutch and making sure both selectors are out of gear for the next few weeks. If I showed up in front of him because of getting hurt for that reason, then I would have eternity to hear about it. Will get it fixed in case somebody else ever tries to use it though. Thanks for the helpful replies, this is the newest tractor I have ever owned by about 25 years, and they are certainly built a bit different in terms of electrical and fuel flow controls. Stuff from the 70's tends to have like 8 wires, one filter, and a mechanical fuel shut off on the pump.