The rest of the story:
Saturday I drove my car into the field and lifted a cylinder to see if I'd be able to lift it. I could, so I pulled them out. Knowing this, I decided to see if I could put it back single-handedly. My neighbor wasn't due home until Monday night.
Stood cylinder on end, put a strap through it to hold it high. Put strap on other end and raised it with one hand while tightening strap with other. Worked fairly nice.
Main issue was the cylinder pivot really wanted to be VERY aligned with the pivot hole before it would go in. This caused some wrestling with it, lowering it, raising it.... cussing a bit. Finally got it in and tightened both straps to hold it.
Repeated same process with second cylinder and got it mounted.
turns out, this was the easy part.
The steel plate that bolts on underneath the cylinders.... well, this was the bugger.
It has four bolt holes so we have a pattern to match. Then, we have the two holes for the pivots of the cylinders.
I had two bolts installed and nothing would line up enough to make anything work. meanwhile, the plate (I'm guessing 50/60 pounds?) was wearing me out since I was trying to lift it while wrestling with it. It fell out of my hands many times. My focus was to not have it fall back on me.
keeping myself intact was pretty high on my list during this process.
finally, I made a quasi-sling so I could try to hold it with the sling while adjusting it with a free hand. This too, basically failed.
I finally took all but one bolt out to lower my alignment points. finally got it started in the right place so added a second bolt and threaded them with the nuts to at least keep the steel plate suspended and my hands free to do other things.
Got it mounted, torqued and greased up.
I also had to put the alternator back on. I took the alternator on this machine and the alternator on the tractor out to be checked out.
so, fixing the cylinders, mounting two alternators cost me the day. I started around 10:00 Saturday morning, quit around 8:00 that night with the hard part done.
Sunday, got up and greased everything and fired it up.
Everything is seeming to work as it should.
Nice side bonus.... the backhoe itself would bleed to the right side of the machine fairly easily. It would hardly ever bleed to the left side, only the right.
I figured I either had to rebuild the cylinders or, the valves (or maybe even both)
Now that I've rebuilt the cylinders, the swing of the hoe is vastly diminished (I mean, you could be on a small slope and just watch it swing 90 degrees in probably 30 seconds)
Now, I've not seen it swing at all but, I've not been on a slope yet. Regardless, if it now swings, I know I have to look at the valves.
Best of all, I still have my 10 fingers and 10 toes. Only a tiny bruise on my thumb nail and one or two on my arm.
I was however, worn out.